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Uranium Enrichment and Fuel Fabrication - Current Issues (France)

(last updated 12 Aug 2008)

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Information about French nuclear fuel cycle plants external link (Nuclear Safety Authority - ASN, in French)
 

General

France issues new regulations for major nuclear facilities

On Nov. 6, 2007, the French Nuclear Safety Authority (ASN) announced the publication of the décret "procédures INB" in the Official Journal of Nov. 3, 2007.

> View ASN release Nov. 6, 2007 external link (in French)
> View Décret n° 2007-1557 du 2 novembre 2007 relatif aux installations nucléaires de base et au contrôle, en matière de sûreté nucléaire, du transport de substances radioactives external link, J.O n° 255 du 3 novembre 2007 page 18026 (in French)

 

No use of reprocessed uranium in French reactors in the near future

The uranium recovered from reprocessing of spent fuel in France is not expected to be used for the manufacture of nuclear fuel in the near future. French utility EdF rather has made provisions for long-term storage of the reprocessed uranium for 250 years. This was revealed in a report of the French Court of Auditors on the decommissioning of nuclear facilities and the management of radioactive wastes.

Usage of the reprocessed uranium (REPU) is problematic for several reasons: since the REPU is contaminated with the artificial uranium isotopes U-232 and U-236, special precautions are necessary during processing: the U-232 and its decay products cause elevated radiation doses for the plant personnel, and the U-236 as a neutron absorber requires higher enrichment levels to achieve the same reactivity. In consequence, use of the REPU is not very attractive at present market conditions: conversion is three times more expensive than conversion of natural uranium, and enrichment cannot be done in France's sole enrichment plant (Eurodif gazeous diffusion plant), since the REPU would contaminate the plant's circuits. For production of two test refueling batches for the Cruas nuclear power plant, the REPU was enriched in a foreign (presumably Russian) centrifuge enrichment plant.

Of the 1050 t of spent uranium oxide fuel annually generated in France, 850 t are being reprocessed at La Hague, at present. (In addition, 100 t of spent MOX fuel arise, which are not reprocessed at all.) From reprocessing of uranium oxide fuel, approx. 816 t of uranium and 8.5 t of plutonium are recovered. Of the uranium recovered, approx. 650 t are converted to the more stable oxide form for long-term storage, awaiting future uses.
The uranium recovered in the former Marcoule reprocessing plant has never been recycled into nuclear fuel at all. It still stays at Marcoule, in the liquid form of uranyl nitrate, 3800 t owned by EdF, and 4800 t owned by CEA and Cogéma.

Cour des Comptes: Le démantèlement des installations nucléaires et la gestion des déchets radioactifs, Rapport au Président de la République suivi des réponses des administrations et des organismes intéressés, Janvier 2005
> Download full report external link (in French)

 


CEA laser-based uranium enrichment research (SILVA)

(programme Silva – Séparation Isotopique par Laser de la Vapeur Atomique)

CEA terminates laser-based uranium enrichment research

France's Commissariat à l'Énergie Atomique (CEA) has completed its research on laser-based uranium enrichment (SILVA programme). The research had been performed from the mid-1980's, co-financed by COGEMA from 1993 to 2002. From 2000 to 2003, an Euro 146 million feasibility study has been performed at Pierrelatte. During this study, some 200 kilograms of enriched uranium (and about one tonne of depleted uranium) have been produced in November 2003.
After COGEMA has made a decision to replace its Eurodif gaseous diffusion plant by centrifuge technology, the SILVA programme will be discontinued. (CEA January 9, 2004)
 

COGEMA MOX fuel fabrication plant, Cadarache (Bouches-du-Rhône, France)

INB No. 32, 54
Information about Cadarache plant external link (Nuclear Safety Authority - ASN, in French)
 

ASN orders CEA to clear former Cadarache MOX fuel plant of all nuclear material by end June 2008

> Download: Décision n° 2007-DC-0036 de l’Autorité de sûreté nucléaire du 21 mars 2007 external link (PDF - in French)

 

ASN upgrades Cadarache MOX fuel plant incident to level 2 on INES scale

The French Nuclear Safety Authority (Autorité de sûreté nucléaire - ASN) has upgraded an incident that occured on November 6, 2006, at Areva's Cadarache MOX fuel plant (Atelier de Technologie du Plutonium - ATPu) to level 2 on the INES scale. A mill used for grinding of MOX fuel rejects (consisting of oxides of depleted uranium and plutonium) had inadvertently been loaded twice, exceeding the criticality criterion for the mill, but fortunately no criticality event was set off. (ASN Jan. 9, 2007)

 

Fabrication of MOX fuel lead test assemblies for the U.S. DOE plutonium disposition program

On Aug. 12, 2003, Cogema has won the contract to fabricate the mixed-oxide (MOX) lead test assemblies (LTAs) for the US plutonium disposition programme. (WNA News Briefing 03.35, Sep. 3, 2003)
> See also: WISE Paris release Sep. 9, 2003 external link: "Transfer" of MOX production capacity from Cadarache to Marcoule: one scandal after another

On Oct. 6, 2003, the U.S. Department of Energy (DOE) applied for an export license (XSNM03327) to export up to 140 kg of plutonium oxide to France for the production of four MOX fuel "lead assemblies". The material will be shipped in July/August 2004 by sea transport from Charleston Naval Weapons Station external link, South Carolina, to Cherbourg, France. For sea transport, two armed Pacific Nuclear Transport, Ltd. (PNTL) ships sailing in convoy will be used. The fabricated MOX fuel assemblies will be returned the same way.
> See also: Federal Register: October 27, 2003 (Volume 68, Number 207)p. 61238 (download full text external link)
On June 15, 2004, the U.S. Nuclear Regulatory Commission denied petitions to intervene filed by Greenpeace International, Charleston Peace, and Blue Ridge Environmental Defense League and directed the Office of International Programs to issue the export license. (SRM-M040615)
On June 16, 2004, the U.S. Nuclear Regulatory Commission issued the requested license for the plutonium export to France (XSNM03327).

On November 7, 2003, the U.S. Department of Energy/National Nuclear Security Administration (DOE/NNSA) amended its January 11, 2000 Record of Decision (ROD) to allow for the fabrication of mixed oxide (MOX) fuel lead assemblies in France on a one-time basis.
> See: Federal Register: November 14, 2003 (Volume 68, Number 220) p. 64611-64614 (download full text external link)

On September 20, 2004, the Pacific Teal and the Pacific Pintail, two UK-registered ships dedicated to the transport of nuclear materials, left Charleston (South Carolina) carrying the plutonium for the MOX fuel lead assemblies to France. (Cogema Sep. 21, 2004)

 

Cadarache MOX fuel factory closed; concerns about possible future use for U.S. plutonium disposition program

The Cadarache MOX fuel factory ceased commercial production on July 31, 2003, due to the high seismic hazard at the site. The capacity of the MELOX plant at Marcoule will be increased to compensate for the closure.
> View ASN release Sep. 3, 2003 external link (in French)

However, according to a WISE-Paris Briefing, there is a possibility that the plant could be used for future production of MOX Lead Test Assemblies for the U.S. plutonium disposition program.

> View WISE-Paris release (July 30, 2003) external link
> Download WISE-Paris Briefing: U.S. "MOX Lead Test Assembly" Controversy: Fabrication at Cadarache, France (July 29, 2003) external link (325k PDF)


 

Cadarache factory will close in late 2002 or early 2003

The Cadarache mox fuel factory, which has been instructed to cease its activity because it does not comply with seismic safety regulations, is expected to close at the end of 2002 or early in 2003, according to the French nuclear safety agency ASN. In case owner Areva does not take the initiative in closing the site down, ASN will carry out the closure with the issue of a decree. (La Tribune- France, Mar 21, 2002)
 

Cadarache Special of Plutonium Investigation newsletter

The April-May 2001 issue of WISE-Paris' newsletter Plutonium Investigation is a Cadarache Special:
> View/download Plutonium Investigation No.20 external link
 

COGEMA confirms plans for closure of Cadarache MOX fuel plant

March 27, 2001: Cogéma confirms that it will close its Cadarache MOX fuel plant in a few years for the earthquake hazard at the plant site. The production of 40 t of MOX fuel is to be relocated to Cogéma's Marcoule plant. The closure might become effective in 2003. (AP March 27, 2001)
 

DSIN inspectors demand shutdown of Cadarache MOX fuel plant for earthquake hazard

July 19, 2000: After five years of fruitless pressure Cogema's external link L'Atelier de technologie du plutonium (ATPu) plant at Cadarache, which produces 40 tonnes of mixed oxide fuel (MOX) per year for export to Germany, government inspectors took the unprecedented step of releasing documents to WISE-Paris external link.
A 1994 survey showed that the area round Cadarache, near the mouth of the river Rhône, had experienced a "significant growth" of seismic activity since the end of 1993, and that "destructive" earthquakes could be expected to recur once a century.
The Directorate for the Safety of Nuclear Installations (Direction de la sûreté des installations nucléaires - DSIN external link) held a meeting with the plant's operators Cogema in 1995, in which it said that "a rapid closure of the installation is necessary." It asked for a "plan for the future of the factory including a definitive closure date not long after 2000". (AFP, The Guardian, WISE-Paris)

> Download WISE-Paris briefing on Cadarache as PDF file external link (84k PDF in French)
> Download Briefing annexes (letters, map, figures) external link (848k PDF in French)
 

Incidents at Cadarache MOX fuel plant

Cadarache events external link (ASN, in French)
 

MELOX MOX fuel fabrication plant, Marcoule (Gard, France)

INB No. 151
Information about Marcoule plant external link (Nuclear Safety Authority - ASN, in French)
 

Spill at Marcoule waste water treatment plant

On July 17, 2007, three cubic meters of waste water with a specific activity of approx. 40 Bq/cm3 spilled inside the building; only some dozen litres reached the outside of the building. The event was rated level 1 on the INES scale.

Violation of criticality rules at MELOX MOX fuel plant

On May 29, 2007, an automatic transport cart carrying plutonium oxide was permitted to enter an already loaded working station. No criticality occured. The incident was rated INES 1. (ASN July 9, 2007)

Government authorizes further capacity increase for MELOX MOX fuel plant

On April 26, 2007, Areva received government approval for the requested capacity increase of the MELOX MOX fuel plant from 145 to 195 tHM/a. (Areva April 27, 2007)

Public Inquiry into further extension of MELOX MOX fuel plant

On Feb. 2, 2006, the Vice Minister of Industry announced the start of the public consultation process regarding the increase of capacity from 145 to 195 tHM/a. The public inquiry will be held from April 18 to June 17, 2006.
> View speech of François Loos, Vice Minister of Industry, Feb. 2, 2006 external link (in French)

MELOX MOX fuel fabrication plant requests further capacity increase

In September 2004, MELOX requested a further capacity increase from 145 to 195 tHM/a. (Areva)

ASN authorizes capacity increase for MELOX MOX fuel plant

On Sep. 3, 2003, the Nuclear Safety Authority (ASN) issued a decree authorizing a capacity increase from 101 to 145 tonnes for the MELOX MOX fuel plant at Marcoule. The increase compensates for the shutdown of the Cadarache MOX fuel plant. According to a COGEMA release of Sep. 4, 2003, the capacity increase is achieved without extension nor major modifications to the plant.

> View ASN release Sep. 4, 2003 external link (in French)
> View Décret n° 2003-843 (Journal Officiel Sep. 4, 2003) external link (in French)
 

Elevated radiation found near MELOX MOX fuel plant

The independent radiation monitoring organization CRIIRAD has found elevated gamma radiation on public roads and in vineyards outside the fence of the MELOX MOX fuel plant at Marcoule (Gard). The radiation exposure is twice background in some places. The radiation source is assumed to be waste stocked on site.

> Download CRIIRAD release Jan. 16, 2003 external link (179k PDF, in French)

On Jan. 14, 2003, Greenpeace France started a campaign of environmental monitoring around the Marcoule plant.
> View Greenpeace press release external link · campaign announcement external link (in French)
 

Public Inquiry into extension of MELOX MOX fuel plant

A public inquiry into the planned extension of the capacity of the MELOX mixed oxide (MOX) fuel plant in Marcoule will be initiated. The capacity increase is required to transfer the capacity of the Cadarache plant to Marcoule. The Cadarache plant is to be closed for its earthquake hazard.
> View ASN release Sep. 26, 2002 external link (in French)

The Ministries of the ecology and of the industry asked the prefect of Gard to open a public inquiry into the demand presented by COGEMA for the extension of the capacity of its MELOX factory of MOX fuel, located in Marcoule.
> View Ecol. Ministry release Oct. 23, 2002 external link (in French)

The public inquiry was set to begin on 8 January, 2003, in the two departements (counties) nearest the plant site at Marcoule. The prefect of the Gard departement external link that contains the Marcoule site announced the opening of the two-month inquiry on 3 December, 2002. (WNA News Briefing Jan. 15, 2003)
 

Incidents at MELOX MOX fuel plant

Marcoule events external link (ASN, in French)
 

COGEMA/SICN nuclear fuel fabrication plant, Veurey-Voroize (Isère, France)

INB No. 65, 90
Information about SICN plant external link (Nuclear Safety Authority - ASN, in French)
The plant halted all production at the end of 2002.

> View more recent issues

COGEMA/SICN nuclear fuel plant license jeopardized by poor safety culture

"From site surveillance visits of inspectors of the Nuclear Safety Authority, the generally low level in the matter of safety culture is known. The licensee has been informed that, if this situation became permanent, it would jeopardize the handling of any nuclear material exceeding the regulatory level of a Basic Nuclear Installation (INB)." (translated from ASN homepage, as of July 22, 2000)
 

Incidents at COGEMA/SICN nuclear fuel plant

SICN fuel plant events external link (ASN - in French)
 

FBFC nuclear fuel fabrication plant, Romans-sur-Isère (Drôme, France)

INB No. 98, 63
Information about FBFC plant external link (Nuclear Safety Authority - ASN, in French)
 

Leak detected in sewage system of FBFC Romans nuclear fuel fabrication plant

On July 17, 2008, Areva notified the Nuclear Safety Authority (ASN) of a break of an underground sewage system for uranium-containing liquids at its FBFC nuclear fuel fabrication plant in Romans-sur-Isère. An inspection held by ASN the same night reveiled that the rupture had occured years ago (!). Areva is currently busy cleaning up the contaminated area. ASN provisionally rated the event INES 1. (ASN July 18, 2008)

> Download detailed report about the incident by independent laboratory CRIIRAD: Commentaires sur l’incident du 17 juillet 2008: détection d’une fuite sur une canalisation à l’usine FBFC-CERCA (AREVA) de Romans-sur-Isère, Note CRIIRAD N°08-149 external link (July 21, 2008, PDF - in French)

FBFC Romans nuclear fuel fabrication plant applies for capacity increase

FBFC - Framatome ANP's fuel subsidiary - has applied for a licence to expand capacity at its Romans fabrication plant. The company's current licence for the Romans plant limits it to 1200 tU in conversion (UF6 to UO2) and 820 tU in pelletizing and assembly. The licence application submitted would increase those limits to 1800 tU for conversion and 1400 tU for pelletizing and finishing operations. FBFC is modernizing the plant to meet new safety and radiation protection standards, partly through the use of more automated processes. (WNA News Briefing 04.05, Feb. 4, 2004)

Incidents at FBFC nuclear fuel fabrication plant

On June 3, 2008, the rules to prevent criticality were violated in the pelletizing workshop. Scrap UO2 material was held in waste containers exceeding the safe mass limit. The event was classified INES 1. (ASN June 20, 2008)

On Nov. 16, 2007, ENUSA (Spain) detected traces of leaked UO2 powder at some containers received from FBFC Romans. The event was classified INES 1.

On May 17, 2004, the rules to prevent criticality were violated: in the conversion plant, the UF6 feed was not interrupted, although the monitoring equipment for the humidity contained in the UO2 powder product was not functioning. However, no criticality occured. The event was classified INES 1.

On July 22, 2003, the rules to prevent criticality were violated: twice the licensed amount of uranium-235 was stored in a cask. No criticality occured. The event was classified INES 1.

On Feb. 21, 2003, the rules to prevent criticality were violated: a cask containing 41 kilograms of enriched uranium powder was stored in an area where only 27 kilograms were permitted. However, no criticality occured. The event was classified INES 1.

 


COGEMA EURODIF enrichment plant, Tricastin (Drôme, France)

Aerial view: Google Maps external link new window

INB No. 93
Information about Tricastin plant external link (Nuclear Safety Authority - ASN, in French)

> See also: Upgrading of French enrichment tails in Russia
> See also: COGEMA EURODIF Georges Besse II centrifuge enrichment plant project, Tricastin (Drôme)
 

French wine appellation "Coteaux du Tricastin" seeks name change after uranium spill

An appellation in the south of France is looking to change its name in order to avoid being associated with a uranium leak at a nuclear power station in the same region. The Coteaux du Tricastin appellation, which neighbours Côtes du Rhône Villages, has resented its association with Tricastin Nuclear Power Centre for some time. Henri Bour, head of the Coteaux du Tricastin appellation, told French news website nouvelobs.com that the region has wanted to change its name 'for about ten years'.
The push for a name change follows the intense media coverage of a uranium leak at the Tricastin nuclear site earlier this month. 'Now, it's useless for a producer to try to sell a bottle of Coteaux du Tricastin - people would laugh in their face,' said Brice Eymard, head of the economic department at the Rhône wine trade body, InterRhône.
A meeting of the administrative appellation council is set for 5 August, where members will discuss the possibility of changing the name Tricastin to Grignan, a local village in the center of the region. (Decanter July 24, 2008)

Uranium-containing waste liquid spills at Tricastin nuclear site

During the night of July 7, 2008, 30 cubic meters of liquid containing 12 grams of uranium per litre (totalling 360 kg of uranium), spilled for unknown reasons from a holding tank at the effluent treatment plant of the Tricastin nuclear site. The effluents seeped into the soil and partly reached the "la Gaffière" river, and then the "le Lauzon" river. The resulting uranium concentration in the "la Gaffière" river was measured at approx. 1000 times normal background. The effluent treatment plant is operated by Areva subsidiary Société auxiliaire du Tricastin (SOCATRI), mainly for the Eurodif enrichment plant. (ASN July 8, 2008)

On July 11, 2008, in a rare move, the Nuclear Safety Authority (ASN) ordered the shutdown of SOCATRI's uranium effluent treatment plant (STEU). At an inspection held on July 10, 2008, ASN had found that the measures taken to prevent any further spills are not satisfactory and that the information given by the licensee to the authority was incomplete. ASN further announced to sue the licensee for the deficiencies identified.
From the announcements made, it is unclear whether the shutdown will have any impacts on the operation of Eurodif's enrichment plant.

On July 16, 2008, the Nuclear Safety Authority (ASN) announced that groundwater and surface water monitoring results had returned to normal except for two locations. Apparently, these higher values are not related to the recent spill, however. A recently completed IRSN study had already identified a few locations with elevated uranium concentrations in groundwater, the source of which has not yet been identified.

> See also related information from

Public enquiry into abatement of flooding hazard at Areva's Tricastin site

Areva intends to perform protective measures against the flooding hazard in case of heavy precipitation at the Tricastin site, in particular from the Gaffière creek crossing the site and from a canal next to the site.
From Feb. 18, to March 21, 2008, the project is subject of a public enquiry held in the surrounding communities. (Areva Feb. 18, 2008)

Unexpected criticality hazard found in Tricastin enrichment plant

During maintenance work, on Dec. 4, 2007, an unexpected deposit of uranyl fluoride (UO2F2) was detected inside a crystallization unit used to fill the enriched uranium hexafluoride (UF6) into the product transport cylinders. The presence of uranyl fluoride in this unit had not been foreseen in the safety analysis of the plant. Such a deposit of uranyl fluoride might lead to a criticality event, in particular in the presence of water. A likely cause for the formation of the uranyl fluoride deposit was the entry of water into the equipment. The event was rated Level 1 on the INES scale. (ASN Dec. 11, 2007, Areva Dec. 6, 2007)

Areva presents study on health risks for residents from operation of nuclear facilities at the Tricastin site

In July 2007, Areva presented a study performed by Institut National de l’Environnement Industriel et des Risques (INERIS) external link in March 2006 on possible health impacts of the operation of the nuclear facilities located at the Tricastin site, in particular the existing Georges Besse I and the future Georges Besse II enrichment plants, the Comurhex conversion plant, and the Socatri and Pierrelatte nuclear fuel facilities. The study investigated only the hazards for residents, limited to the hazards from chemical toxicity occuring during regular operation of the facilities. According to the study, none of the risks investigated are causing concern.

> Download Etude d’évaluation des risques sanitaires (ERS) external link (in French)

Évaluation des risques sanitaires liés au fonctionnement des établissements AREVA de la plateforme du Tricastin: usines Georges Besse I et II, SOCATRI, COGEMA Pierrelatte et COMURHEX (1er niveau d'approche), Bilan des études sanitaires, Rapport final, par Corinne MANDIN, Institut National de l’Environnement Industriel et des Risques (INERIS), Mars 2006

Regulator cites Eurodif for failure to report criticality-related event in enrichment plant

By letter dated March 29, 2007, the Nuclear Safety Authority (ASN) demands an explanation from Eurodif, why the violation of a criticality-related criterion had not been reported to the authority. In January 2007, the boron concentration in the cooling water of the enrichment cascades had fallen below the permissible level. This might have resulted in a criticality excursion (an uncontrolled chain reaction accompanied by heavy radiation releases) in the plant. While Eurodif restored the boron concentration upon discovery of the condition, Eurodif failed to report the event to ASN. This failure was only discovered by ASN during an inspection on March 26, 2007.

Kazatomprom to obtain share in French enrichment plant in exchange for uranium deliveries?

> See here

Elevated radiation found around Tricastin nuclear site

The independent radiation monitoring group CRII-RAD identified external radiation doses up to 20-fold above natural background at several locations around the Tricastin site of nuclear installations. The site comprises, among others, the Eurodif enrichment plant. CRII-RAD suggests that the source of the excess radiation observed is nuclear material stockpiled on site.

> View CRII-RAD release Oct 8, 2002 (in French) external link
> Download CRII-RAD monitoring results external link (PDF, in French)

France to abandon development of atomic vapour laser enrichment technology

Development of the Silva atomic vapour laser isotope separation process will cease by 2003, the Commissariat à l'Energie Atomique (CEA) external link announced. Instead, the CEA will resume R&D work on gas centrifuge enrichment technology that was suspended in 1983, when research efforts were focussed on laser enrichment technology. CEA Administrator General Pascal Colombani said that Silva proved 'difficult to implement and had an uncertain commercial future'. (UI News Briefing 01.07, Feb. 14, 2001)

Incidents at Tricastin enrichment plant

Tricastin events external link (ASN, in French)
 

AREVA/COGEMA EURODIF Georges Besse II centrifuge enrichment plant project, Tricastin (Drôme)

Suez acquires an equity stake in Areva's new Georges Besse II centrifuge uranium enrichment plant

Suez external link and Areva have signed an agreement giving Suez 5% ownership interest in the company that holds the Georges Besse II uranium enrichment plant. Suez, through its Energy Services business line, is building the electrical installations, and supplying the fluid management systems and the HVAC and process cooling equipment of the new plant, which is scheduled for startup in 2009. With the agreement, Suez will be able to secure a portion of its nuclear reactor supply needs in enriched uranium. Georges Besse II is one of France's largest current industrial investments, representing a total of close to EUR 3 billion. (Suez/Areva Jun. 3, 2008)

Areva presents study on health risks for residents from operation of nuclear facilities at the Tricastin site

> View here

Construction commences at Georges Besse II centrifuge enrichment plant

Construction of the first section of the Georges Besse II centrifuge enrichment plant has commenced. First production is expected in 2009. (Le Dauphiné Libéré, 29 Oct. 2006)

Areva and Urenco announce creation of Joint Venture ETC (Enrichment Technology Company)

On July 3, 2006, Areva and Urenco signed the agreement to settle ETC (Enrichment Technology Company), the Joint Venture between Areva and Urenco in the field of uranium enrichment centrifuge technology. The Joint Venture is now effective with the acquisition by Areva of a 50% equity stake in ETC. This opens the way for the construction of the new Georges Besse II enrichment plant. (Areva July 3, 2006)

Kazatomprom to obtain share in French enrichment plant in exchange for uranium deliveries?

> See here

Dutch parliament to vote on agreement giving Areva access to Urenco's centrifuge enrichment technology

In March 2006, the lower house (Tweede Kamer) of the Durch parliament will vote on the Cardiff Agreement which will give Areva/Cogéma access to Urenco's centrifuge enrichment technology, while excluding access to classified design information. The agreement extends the 1970 Almelo Treaty which is the basis of the trilateral Urenco consortium. The agreement, while excluding the enrichment of uranium for nuclear bombs, would allow for the enrichment of uranium for France's nuclear navy.
In the United Kingdom, the Cardiff Agreement was presented to Parliament in October 2005 and ratified before the end of the year. (Nuclear Fuel Jan. 16, 2006)
The German government approved the Cardiff Agreement on October 15, 2005; involvement of parliament was not deemed necessary. (MdB Johannes Pflug, Feb. 15, 2006)

Agreement between the governments of the United Kingdom of Great Britain and Northern Ireland, the French Republic, the Federal Republic of Germany and the Kingdom of the Netherlands regarding collaboration in centrifuge technology: Cardiff, 12 July 2005 external link (UK Foreign and Commonwealth Office - 399k PDF)

European Commission approves Areva/Urenco centrifuge enrichment venture

On Oct. 6, 2004, the European Commission decided that French government-owned Areva may acquire a stake in Urenco's subsidiary Enrichment Technology Co Ltd (ETC). The approval was given on the condition that the companies would act independently on capacity increases, and that Euratom surveillance would be strengthened. (Dow Jones Oct. 6, 2004)

COMMISSION DECISION of 06.10.2004 declaring a concentration to be compatible with the common market and the functioning of the EEA Agreement (Case No COMP/M.3099 – Areva/Urenco/ETC JV) external link (276k PDF)

Public Debate on Eurodif centrifuge enrichment plant project

From 1 September to 22 October 2004, a public debate was held in the departments of Drôme, Gard, Vaucluse, and Ardèche, neighbouring the planned centrifuge enrichment plant "Georges Besse II" in southern France.

Débat public sur le projet Georges Besse II external link (in French)
> Download: Le dossier du maître d'ouvrage external link (in French)

> See also: Communiqué du Réseau Sortir du nucléaire (1 Sep 2004) external link (in French)

European Commission extends probe into Areva/Urenco venture

The European Commission has launched a detailed investigation into Areva's proposed acquisition of a 50% stake in Enrichment Technology Company (ETC). At this stage, the Commission is concerned that the joint venture may result in less R&D with regards to centrifugation technology and lead to higher prices for enriched uranium used for fuel in nuclear power plants. (European Commission June 22, 2004)

AREVA secures Urenco's gas centrifuge technology and launches new enrichment plant project

COGEMA's parent company AREVA Group signed an agreement with URENCO shareholders on Nov. 24, 2003, under which it will acquire a 50% equity interest in Enrichment Technology Company (ETC). ETC comprises all of URENCO's centrifuge design and manufacturing activities as well as its R&D in the field of centrifuge equipment and installations for uranium enrichment to produce nuclear fuel.
A new enrichment plant, to be named Georges Besse II, will be built at the Tricastin site with a total investment around EUR 3 billion. Production capacity will be increased gradually starting in 2007 and reach its nominal level around 2016. The actual construction is expected to get under way in early 2005, once government authorizations have been obtained and relevant international treaties have been modified allowing AREVA to take an equity interest in ETC. This is supposed to be done in the 4th quarter of 2004. (Areva Nov. 26, 2003)

COGEMA considering new centrifuge enrichment plant at Tricastin (France)

COGEMA's parent company AREVA made a first step to abandon uranium enrichment by gaseous diffusion. In a Memorandum of Understanding, URENCO and AREVA have agreed to develop plans for working together in the field of centrifuge technology for uranium enrichment. The companies envisage a 50-50 joint venture to build a new centrifuge enrichment plant that would progessively replace the existing Tricastin plant capacity beginning from 2007. (Areva/Les Echos Oct 9, 2002)

"COGEMA's enrichment subsidiary Eurodif, reportedly in partnership with Japan Nuclear Cycle Development Institute, is considering building a centrifuge enrichment facility at COGEMA's Tricastin site. Yves Coupin, head of COGEMA's uranium division, stated that additional centrifuge units would 'complement' the existing gaseous diffusion units and allow more flexibility in adjusting capacity to meet market demand. Coupin also said that initial SILVA capacity under the joint COGEMA/CEA laser enrichment research venture could come into operation before the end of next decade." (UI News Briefing 98.44, see also FreshFUEL 11/9/98 external link)


 


Comurhex uranium conversion plant, Malvési (Aude, France)

Aerial View: Google Maps external link new window

 

Railcar with Yellow Cake shipment for Malvési conversion plant overloaded

A railcar carrying uranium ore concentrate from the Hamburg harbour (Germany) to the Comurhex conversion plant at Malvési was found to be overloaded when entering France at Apach. The railcar carried 68 t rather than the permitted 61 t. (Saarbrücker Zeitung Aug. 13, 2008)

Leaking Yellow Cake container arrives at Comurhex Malvési uranium conversion plant

On July 26, 2007, a small spill of Yellow Cake was detected during the unloading of a container from a railcar at Comurhex's Malvési conversion plant. The container held 36 barrels of natural uranium concentrate (Yellow Cake) produced in Niger. It turned out that one of the uranium barrels was damaged and around 30 kg of Yellow Cake had spilled inside the container. Traces of spilled uranium were also found on the ship that had carried the container before the rail transport. The event was rated Level 1 of the INES scale. (ASN Aug. 9, 2007)

Areva increases capacity at Comurhex Malvési conversion plant

On May 21, 2007, Areva announced that it is to spend EUR 240 million to build new facilities and expand existing facilities at its Comurhex Malvési conversion plant. First industrial production is scheduled for 2012, based on 15,000 metric tons of uranium per year. This figure may be increased to 21,000 tons to meet market requirements.

CRIIRAD finds unexpected radionuclide concentrations in slurries at Comurhex Malvési plant

On Nov. 14, 2006, the independent radiation laboratory CRIIRAD released a report giving the results of a radiation survey conducted at the Malvési conversion plant on Sep. 21 and 22, 2006. The slurries contained unexpected high concentrations of thorium-230, which might lead to inacceptable radiation doses from inhalation. Moreover, the artificial nuclide americium-241 was identified, probably caused from former processing of recycled uranium.

> Download related CRIIRAD documents external link

IRSN demands cleanup of soil contaminated from spills at Comurhex Malvési plant

On July 25, 2006, the Institut de Radioprotection et de Sûreté Nucléaire (IRSN) external link performed a radiation survey of areas outside the Comurhex Malvési plant. It turned out that several areas were contaminated from uranium decay products (Th-234 and Pa-234m in particular) released during spills. IRSN demands the cleanup of those areas. (Compte rendu d'intervention, IRSN, Oct. 2006)

New spill of slurries at Malvési conversion plant went undetected for one month

On June 20, 2006, a spill of an unreported amount of contaminated slurries occured from leaking pipework connecting decantation basin B5 with the treatment plant for the supernatant liquids. The spill covered a surface area of 350 square meters and was only detected on July 19, 2006. (Compte rendu, Comité Local d'Information et de Concertation, Séance du 24 Juillet 2006 à Narbonne)

Production halted at Malvési conversion plant after new spill and for decantation pond dam failure hazard after heavy rain

On January 30, 2006, Comurhex had to halt parts of its production at Malvési due to heavy rainfall in the area. According to a Comurhex press release, the production halt was a preventive measure necessary to maintain a safety margin in the plant's effluent decantation ponds. (Comurhex Jan. 30, 2006)
However, during heavy rain on Jan. 28 - 30, 2006, precipitation came into contact with the slurries still lying outside of the B2 dam broken in 2004 (according to Comurhex, bad weather had prevented the reconstruction of the dam). An unspecified amount of the contaminated liquid (carrying high loads of nitrate) then spilled into the canal of Tauran. (Compte-rendu du CLIC Malvési, Comurhex-Narbonne, 16 février 2006)
On March 5, 2006, strong winds resulted in an overflow of several decantation ponds due to insufficient safety margins of the ponding water levels, leading to another spill of an unspecified amount of nitrate-contaminated waters to the canal of Tauran. During the period from end-January to mid-April, the amount of nitrate released by Comurhex (297 t NO3) was six times higher than in a complete year without incidents (46 t NO3). The release of uranium during that period (75 kg U) was only slightly higher than in a complete normal year (63 kg U). (Compte-rendu du CLIC Malvési, Comurhex-Narbonne, 22 mai 2006; AREVA: CLIC du 22/05/06: Bilan des intempéries, Actions d’amélioration)
Production was resumed on April 1, 2006.

Dam failure of decantation pond at Malvési conversion plant

On March 20, 2004, a dam failure at decantation and evaporation pond B2 of the Malvési conversion plant released approx. 30,000 cubic metres of liquid and slurries. The liquid contained high concentrations of nitrate and led to elevated nitrate concentrations of up to 170 mg/L in the canal of Tauran for several weeks, while uranium concentrations remained unchanged. The dam failure is believed to be caused by an "abnormal presence of water" due to heavy rain in summer 2003. (Rapport environnemental, social et sociétal 2004, COMURHEX Malvési)
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Derailment of railway car carrying uranium ore concentrates

On September 23, 2001, a railway car carrying 30 tonnes of uranium ore concentrates derailed at the Courbessac shunting yard near Nîmes (Gard) in Southern France. The uranium obviously originated from Niger. It was shipped via Benin and Britanny to the Comurhex conversion plant at Malvési near Narbonne (Aude). No uranium was spilled. (Midi Libre Sep 25, 2001)

Fire on railway car carrying uranium ore concentrates

On June 8, 2000, a beginning fire was detected on a railway car carrying uranium ore concentrate (magnesium uranate) from Niger to Malvési. The fire was noticed at the entry of the Chantenay station (near Nantes) and the train was stopped. Fire brigades extinguished the fire within minutes. (ASN)
 

Comurhex uranium conversion plant, Pierrelatte (Drôme, France)

Aerial view: Google Maps external link new window

INB No. 105
Information about Comurhex plant external link (Nuclear Safety Authority - ASN, in French)
 

Uranium leak in sewage system of Comurhex Pierrelatte conversion plant

On Aug. 22, 2008, Areva reported a minor leak in the sewage system of the Comurhex Pierrelatte conversion plant. The amount of uranium escaped is believed to be on the order of 250 grams.

Areva presents study on health risks for residents from operation of nuclear facilities at the Tricastin site

> View here

Areva increases capacity at Comurhex Pierrelatte conversion plant

On May 21, 2007, Areva announced that it is to spend EUR 370 million to build new facilities at its Comurhex Pierrelatte conversion plant. First industrial production is scheduled for 2012, based on 15,000 metric tons of uranium per year. This figure may be increased to 21,000 tons to meet market requirements.

Uranium spill at Comurhex Pierrelatte conversion plant

On December 3, 2003, about 150 grams of uranium were inadvertently released into the rainwater collection system of the Comurhex Pierrelatte plant.

> View ASN release, Jan. 28, 2004 external link (in French)

ASN cites Comurhex on deficiencies at Pierrelatte conversion plant

On Oct. 29, 2003, the French Nuclear Safety Authority (ASN) issued a citation to Comurhex on deficiencies regarding fire prevention at its Pierrelatte uranium conversion plant.
> View ASN release Oct. 29, 2003 external link (in French)
> Download ASN citation Oct. 29, 2003 external link (PDF - in French)

Pierrelatte uranium conversion plant flooded

During the night from 19 to 20 October, 2001, a water leakage flooded the Comurhex uranium conversion plant at Pierrelatte. The plant was not in operation at that time. The water became contaminated with traces of residual uranium from the floor and the walls of the facility. A part (approximately 200 cubic meters) of the contaminated water flowed into the surroundings of the building. The maximum uranium concentration found in the water was 2 milligrams per litre. The event was rated Level 1 of the INES scale. (ASN 31 Oct 2001)

Dumping of uranium conversion waste near Pierrelatte stopped

A total of 100,000 casks containing low-level radioactive waste from the Comurhex uranium conversion plant at Pierrelatte in Southern France have been dumped in a domestic waste deposit in the nearby community of Solérieux (Drôme dept.). In the Pierrelatte plant, Comurhex, a COGEMA subsidiary, is converting UF4 to UF6 for later enrichment in the Eurodif plant. The wastes consist of calcium fluorine, contaminated with uranium. The amount of wastes dumped was 1000 tonnes per year.
After the situation had been made public by MP Michèle Rivasi, Comurhex decided to stop dumping at Solérieux and to keep the wastes on site at Pierrelatte for intermediate storage, until a proposed national low-level waste facility will be operable in 2002.
Sources: Le Monde 22 Jul 1999, Nuclear Fuel 26 July 1999, dpa 3 Aug 1999
> View map external link new window (ANDRA)
 

Incidents at Comurhex Pierrelatte conversion plant

Comurhex Pierrelatte events external link (ASN - in French)
 

Cogéma Pierrelatte TU5 conversion facility for uranyl nitrate (Drôme, France)

INB No. 155
Information about TU5 plant external link (Nuclear Safety Authority - ASN, in French)
 

Areva presents study on health risks for residents from operation of nuclear facilities at the Tricastin site

> View here

Criticality rules violated at TU5 conversion facility

On June 30, 2006, Areva notified the Nuclear Safety Authority ASN that concentrations of uranium-235 in excess of the licensed 1% had been found in several drums. On July 18, 2006, ASN ordered Areva to take urgent measures to assure the licensed level in all drums. (ASN July 18, 2006)
 

Explosion in TU5 conversion facility

On March 16, 2002, a 200-litre tank of low-level liquid radioactive waste exploded at Cogéma's Pierrelatte TU5 conversion facility. An investigation done by the Nuclear Safety Authority ASN revealed two handling errors which had led to the mixing of chemically incompatible liquids in the tank. The explosion caused no injuries and no releases to the environment. The event was classified level 1 on the INES scale. (ASN April 10, 2002)
The plant processes recycled uranium from the La Hague reprocessing plant from the chemical form of UO2(NO3)2 (uranyl nitrate) into U3O8.
 

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